The motors of these old tractors had sleeves in them, luckily. [see picture one.] We had to rob a couple of the ones out of the really old tractor to rebuild the 1927 one, as one was scored really grossly, and one had deep rust pits at the ring line. The crankshaft had no counterweights on the '27 motor, so we used the weighted '22 crank. There were shims under the rod caps, so we just tightened the bearings up a wee bit, added new piston rings out of Boston, honed the chosen liners, and put her together. I had taken the head to a machine shop, and they manufactured some new valves, seats and guides, [Caterpillar valves, small block Chevy guides and homemade seats]. Anyhow, the head went back on and worked nicely.
When we put the pulley on, --- a very simple task, we had a problem, [picture two]. When we got the tractor running, the pulley seemed to whine. with the pulley off there was no noise, [picture 3]. We deciphered that some small misalignment inside on the pulley shaft, telegraphed out the pulley shaft and the pulley acted like a bell, amplifying the vibration. I made a sound deadener out of plywood to stop the sound, or at least soften it. I have not tested this weird solution. The big wooden washer is just inside the spokes on the pulley.
Oh, I almost forgot, about the radiator cap I have been bragging about. [pictures 4 & 5].